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Fix'n a Vixen
Part III
By Scott Hraska
After a ton of grinding and fiberglassing it was time
for some finishing bodywork and paint. My father and I brought the boat over
to Ronnie’s house for a paint job.
When we got there I thought the boat
was just about ready to paint. Boy was I wrong! I wasn’t even prepared for
all the sanding that we had to do to make the boat look good when painted.
After 2-3 weeks of rough sanding (80-100 grit), Ronnie worked his magic for
the finishing bodywork. He didn’t want my father or myself to even try to
help because he would just have to go over it again (which was true). At
first I didn’t understand really but I soon realized how perfect the boat
must be before paint.
It was about 2 more weeks before Ronnie was ready to
paint the bottom. My father and I stood outside the garage and watched as
the blue metal flake was sprayed on. It
looked so amazing, finally I knew all my fathers hard work, Ronnie’s, and
my own would be paying off in the near future.
Once the bottom was all
painted and cleared my father and Ronnie’s each grabbed one side of the
boat and I grabbed the nose and we just picked it up, flipped it over and
placed it back on the trailer. Ronnie did a little more sanding and then
sprayed the top metallic blue also. He called it “dumpster paint”
because his friend was throwing it out after sitting on the shelf for like
10+ yrs. It worked awesome though and came out great!
My father and I towed the boat
home to put the floor in and begin rigging.
We also added little braces
in-between the stringers to make the boat even more rigid. The floor was
glassed down over the stringers and then covered with 2 layers of bi-axial
fiberglass.
Once everything was dry I painted the inside of the boat with
outdoor paint just to make sure its all sealed up nice. After that we
started on the wiring. That took about 2 ½ weeks to complete to what I
thought was good.
We had an idea of a windshield
that we made out of some thick paper. I went out looking for some lexan
shops but found I didn’t have enough $$ for it. I ended up using just
tinted Plexiglas. My father and I (mostly my father) made a skeleton mold to
form the windshield with.
I borrowed a pair of my neighbor’s fireman
gloves and stood in front of our 110,000btu kerosene heater with this sheet
of Plexiglas and some gloves. (Keep
in mind this is in the middle of the winter in NY - temps were in the low
teens).
Once it got nice and pliable I would run over and push it over on
the mold. I repeated this process for a few days until I liked the shape.
Next was the trimming and fitting. That took a week or 2 just because it’s
so hard to make it fit the curved shape of the vixen’s deck. Once it fit
nice we screwed it down and sealed it on with 5200 black marine sealant. I
love the way it came out and really think it gives the boat a “sleeker”
look.
Next up was the carpet. We
went to Home Depot a few weeks earlier and ordered up 12ft of charcoal
grayish carpet. Once it arrived we began fitting it so there was the least
amount of seams possible. Once the carpet was cut and fitted it only took
about ½ hour to glue down. We were originally going to carpet the transom,
the transom knees and the back of the boat but decided it was not needed.
The original molding inside the boat was missing a 2 ft
section. We couldn’t find a match for it so instead of using push molding
we decided to use aluminum and rivet it up. It only took one night for that
and it came out better then I expected.
Back out to Ronnie's the boat
went to get the final rigging. Once the boat was out by Ronnie's again the
holes were drilled and the jack plate was mounted. Then taken off and sent
out to be powder coated. In the meantime, the holes for the steering were
cut. When I went out to Ronnie's one day I found all my wiring laying on the
floor. It turns out that he didn’t like it, but that’s fine with me. Its
OK though because the wiring job he did is 10X better then mine. Now I know
how to do it next time J.
Just about all that was left
was to cut down the lower unit, and find a way to make the midsection fit. I
bought this mid (2cyl) off ebay for $40 and thought it was perfect. It turns
out that Ronnie had to mill the top off that one, and the top of one of my 3
cylinder mids and then re-weld the 3cyl top on the 2cyl. mid. This was
because on 2 cylinder motors there is a different bolt pattern on the power
head. I gave Ronnie a bunch of aluminum and he welded up an AWESOME looking
snout off the back of the mid (really sounds cool).
Over the winter my mom and her
friend re-covered the seats I acquired from Ronnie. They did an amazing job
with the white pleats and blue stripe down the middle- it's just what I
wanted J
so while my dad and Ronnie were wiring up the last bits on the motor, I was
bolting down the seats and the gas tank.
Eventually it was time to
start the engine and man did it sound like crap! I know it’s an OMC and
all but still…something wasn’t right. We took the boat out and I
couldn’t even get up on plane, but the trip was successful because I wasn’t
towed in! We found out that the
hi-speed jets were clogged shut, which is why I had no power at all. We
re-built all 3 carbs and took the boat out again. It got on plane but still
had a lot of trouble doing it...and still sounded really flat…. like it
was losing power somehow??
With the suspicion that the
motor was sucking in water we pulled the head to find that indeed water was
leaking in. We moved on to the exhaust cover. It turns out that ALL 3
gaskets were junk and the motor was sucking in tons of water. After
replacing all the gaskets the motor ran AWESOME. I saw a top speed of 56.1
on the GPS first day of testing.
After messing with the motor
height and some props, the best I’ve seen is 60.4 mph on the GPS. The
first prop was a cleaver I bought off Ebay for $50 - it’s a solid hub OMC cleaver (dimensions unknown) and it
turned about 6500-6700 rpm. The most
recent prop is a cut down V-6 chopper that’s 13 ¾ X 26 with a good amount
of cup; I turn that prop to about 6000 at 60.4 mph. Keep in mind this is only
with an old junky 1985 70hp that was used on a 2000lb Boston Whaler for
years before I got it from my uncle. I can’t wait to get some real power
out of this baby! I’ll keep
you updated on my progress J
This section
features articles written by you guys. Submit whatever you would like - as long as
it applies to HydroStreams, motors, trailers, or towing vehicles. Please send it to
me in a form where I can just insert it into this page (some kind of Word processing
document would be good). It would be a good idea to check with me first to make sure
nobody else is working on the same topic. Everyone please consider writing
an article and sharing some information that will
help out your fellow Streamers.
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